What have you done to your car today?

Soldato
Joined
5 Oct 2009
Posts
13,839
Location
Spalding, Lincs
Yes! it let go while sending it in 4th gear, will pull out the piston and rod tomorrow, going to fit a spare engine when i can find one and get this one rebuilt later in the year with some forged rods etc.

Gutted! Excuse for upgrades are always good though!

Broke it.

Starter died.

Melted the wire in the main harness all he way to the battery area.

Great

Wow, that's a pretty catastrophic started failure so make that happen!
 
Soldato
Joined
3 Jun 2012
Posts
10,835
Gutted! Excuse for upgrades are always good though!



Wow, that's a pretty catastrophic started failure so make that happen!

Yea, to fix it I'm going to have to strip the front of the engine down to release the harness, then undo the insulation on the harness and then replace the wire. So how redo the insulation and fit a new starter motor.

Or... I could look for where it terminates up top, chop it and route a new wire to the starter and just leave a dead bear wire in the harness. The car seemed to bump start OK and drive with no code so fingers crossed no other wires are damaged.
 

Ev0

Ev0

Soldato
Joined
18 Oct 2002
Posts
14,152
Those dials have come out lovely!

I need to do mine, car is only 4 years old but it bugs me that the plastic is all swirly.

Only polish stuff I’ve got in at the moment is some old megs scratch x (Not the v2, the old stuff), not sure if that’d be any good?
 
Don
Joined
18 Oct 2002
Posts
41,752
Location
Notts
Gave it a good fettle yesterday

Looking good for 7 years old and 84k miles :)

93122397_10157018884816847_2977808058765279232_o.jpg
93000485_10157019174371847_3066749517136134144_o.jpg
 
Soldato
Joined
4 Sep 2003
Posts
4,426
Location
Cornwall
Looks great Rotty.

Just fitted a new air intake hose on the 350gt. Thought it'd be a 2 minute job, turns out because the new silicone one doesn't compress like the oem rubber one I had to spend nearly an hour dismantling and re-assembling half the engine bay to squeeze it in :p
 
Associate
Joined
20 Oct 2002
Posts
1,147
Location
Northampton
a follow up on yesterdays findings, the rod is out and has a slight bend. :D

ortLVQI.jpg

I have had a look at the block and the oil squirter that was hitting the piston is still in place so im confident the block can rebuilt. probably have to get re-bore with some oversized pistons and forged rods!
 
Caporegime
Joined
26 Aug 2003
Posts
37,506
Location
Leafy Cheshire
Did a pretty good service on the TT today, oils (both Engine and DSG), filters, brake pads and disks, and started on tired bushes. Still got new rear shocks to go on (one is well past it’s best) as well as possibly doing the fronts (but not ordered these yet). Also had chance to clean the engine bay, which was terrible!

tt-enginebay.jpg
 
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